Sadly 401 has been out of service for longer than we expected whilst we are waiting for the delivery of some new fusible plugs before the loco can be steam tested and re-enter service. After the locos boiler washout the opportunity was taken to carry out some extra jobs:
401s blowdown valve crank handle - this has had the curve removed and shortened slightly |
Ready for welding |
Michael cutting a section out of the blowdown valve's operating handle in order to shorten it |
Annealing the copper washer which sits in the centre of the blowdown valves gasket |
Blowdown fully open, now much easier and safer to operate |
The locker in the cab has received a clean out, needle gun and re-paint, seen here in primer |
After undercoating (sadly no photo), it was given two top coats of white gloss |
Another minor job, repainting the metal plates on the cab floor (after photo below) |
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